novaderrik
Jun 19th, 03, 12:19 AM
tonight (this morning?) at 3am i was making the 15 mile trek home from work in the Nova, and kind of got on it a little bit at a stop sign- no big deal, tach never saw the high side of 4000 rpm. get up to cruising speed around 60 mph, and all of a sudden the car kind of starts running crappy and making an awful thunk thunk thunk sound. first thought- "****E , i blew it up!!" pull over, and it idles really rough, and all of a sudden the noise stops and the idle smoothes out. nothing seems wrong, figured it was the Gods playing mind games with me in the middle of nowhere, and i leave. it kind of misses under load, but no big deal for the 6 miles to my house. good oil pressure and temp stayed at 185 like always, and no knocking noises. get it in the shop and run a compression test- 180-195 on every cylinder but #1, which was zero. pull that valve cover off and see the #1 exhaust rocker kind of sitting on the stud, and no pushrods in sight on either intake or exhaust on that cylinder. pull the intake, and the intake pushrod is laying under the roller lifter "spider" thing in a nice lightning bolt shape, and the exhaust pushrod is kind of sticking up thru the hole a litle bit and still straight to the naked eye.
my theory- the exhaust rocker poly lock let loose, and the nut spun off (intake poly lock was still tight, but the pushrod was all mangled in the valley). the exhaust pushrod went flying and took out the intake pushrod and sent it into the valley- that was the noise- a pushrod getting banged around and screwed up. damage is minimal- 2 pushrods and rockers, and a new set of intake gaskets. about $100 thru my GM connection, i think. could have been MUCH worse- could have trashed my $3500 engine (after only 3 years and about 30,000 miles) and i could have had to walk home...
i took pics of the carnage, but need to upload them to my webshots page yet. maybe around noonish or so after i get some sleep.
my theory- the exhaust rocker poly lock let loose, and the nut spun off (intake poly lock was still tight, but the pushrod was all mangled in the valley). the exhaust pushrod went flying and took out the intake pushrod and sent it into the valley- that was the noise- a pushrod getting banged around and screwed up. damage is minimal- 2 pushrods and rockers, and a new set of intake gaskets. about $100 thru my GM connection, i think. could have been MUCH worse- could have trashed my $3500 engine (after only 3 years and about 30,000 miles) and i could have had to walk home...
i took pics of the carnage, but need to upload them to my webshots page yet. maybe around noonish or so after i get some sleep.